Following the recent incident where my engine stopped working because an inlet valve seat dropped out, I have now stripped the head and drawn some conclusions about what happened.
It turns out that the affected cylinder is the same one in which a seriously burnt exhaust valve was found to be the the most likely cause for the car having been taken off the road years before and which then lead to it becoming (cover his ears) a basket case. Here is what it looked like then:
KNO_5846 by Peter Thompson, on Flickr
Obviously I put a new valve in at the time, but I didn't consider it necessary at the time to have the seat re-cut...maybe I should have done? So it was thoroughly ground-in, which possibly was a mistake.
Today I had to tap the inlet seat back in to allow me to compress the springs to get the valve out. But then the real culprit was obviously this same exhaust valve. It has really badly recessed the seat and burnt away at one side. I think that some of the crusty deposits in the combustion chamber might even be melted metal.
MAL_3578 by Peter Thompson, on Flickr
MAL_3586 by Peter Thompson, on Flickr
So for me running the number of miles at the speed have been doing without an unleaded conversion to the head was a mistake. I will definitely have the conversion done if I rebuild the engine and for any future engine jobs.
It explains the strange putt-putting noise the exhaust started making a few months ago, how I was so overly intrigued that my rebuilt engine had such a nice sound in comparison and why the engine had become such a pig to cold-start.
It doesn't explain why only a few days prior to giving up on me, the engine seemed to be running better than it had ever done.
It turns out that the affected cylinder is the same one in which a seriously burnt exhaust valve was found to be the the most likely cause for the car having been taken off the road years before and which then lead to it becoming (cover his ears) a basket case. Here is what it looked like then:
KNO_5846 by Peter Thompson, on Flickr
Obviously I put a new valve in at the time, but I didn't consider it necessary at the time to have the seat re-cut...maybe I should have done? So it was thoroughly ground-in, which possibly was a mistake.
Today I had to tap the inlet seat back in to allow me to compress the springs to get the valve out. But then the real culprit was obviously this same exhaust valve. It has really badly recessed the seat and burnt away at one side. I think that some of the crusty deposits in the combustion chamber might even be melted metal.
MAL_3578 by Peter Thompson, on Flickr
MAL_3586 by Peter Thompson, on Flickr
So for me running the number of miles at the speed have been doing without an unleaded conversion to the head was a mistake. I will definitely have the conversion done if I rebuild the engine and for any future engine jobs.
It explains the strange putt-putting noise the exhaust started making a few months ago, how I was so overly intrigued that my rebuilt engine had such a nice sound in comparison and why the engine had become such a pig to cold-start.
It doesn't explain why only a few days prior to giving up on me, the engine seemed to be running better than it had ever done.